Abstract: This paper provides a comprehensive study pertaining to diagnosis of intermittent high vibrations on an industrial gas turbine using detailed vibrations analysis, followed by its rectification. Engro Polymer & Chemicals Limited, a Chlor-Vinyl complex located in Pakistan has a captive combined cycle power plant having two 28 MW gas turbines (make Hitachi) & one 15 MW steam turbine. In 2018, the organization faced an issue of high vibrations on one of the gas turbines. These high vibration peaks appeared intermittently on both compressor’s drive end (DE) & turbine’s non-drive end (NDE) bearing. The amplitude of high vibration peaks was between 150-170% on the DE bearing & 200-300% on the NDE bearing from baseline values. In one of these episodes, the gas turbine got tripped on “High Vibrations Trip” logic actuated at 155µm. Limited instrumentation is available on the machine, which is monitored with GE Bently Nevada 3300 system having two proximity probes installed at Turbine NDE, Compressor DE &at Generator DE & NDE bearings. Machine’s transient ramp-up & steady state data was collected using ADRE SXP & DSPI 408. Since only 01 key phasor is installed at Turbine high speed shaft, a derived drive key phasor was configured in ADRE to obtain low speed shaft rpm required for data analysis. By analyzing the Bode plots, Shaft center line plot, Polar plot & orbit plots; rubbing was evident on Turbine’s NDE along with increased bearing clearance of Turbine’s NDE radial bearing. The subject bearing was then inspected & heavy deposition of carbonized coke was found on the labyrinth seals of bearing housing with clear rubbing marks on shaft & housing covering at 20-25 degrees on the inner radius of labyrinth seals. The collected coke sample was tested in laboratory & found to be the residue of lube oil in the bearing housing. After detailed inspection & cleaning of shaft journal area & bearing housing, new radial bearing was installed. Before assembling the bearing housing, cleaning of bearing cooling & sealing air lines was also carried out as inadequate flow of cooling & sealing air can accelerate coke formation in bearing housing. The machine was then taken back online & data was collected again using ADRE SXP & DSPI 408 for health analysis. The vibrations were found in acceptable zone as per ISO standard 7919-3 while all other parameters were also within vendor defined range. As a learning from subject case, revised operating & maintenance regime has also been proposed to enhance machine’s reliability.
Abstract: In this study which has been conducted in Akçasu
Forest Range District of Devrek Forest Directorate; 3 methods (weed
control with labourer power, cover removal with Hitachi F20
Excavator, and weed control with agricultural equipment mounted on
a Ferguson 240S agriculture tractor) were utilized in weed control
efforts in regeneration of degraded oriental beech forests have been
compared. In this respect, 3 methods have been compared by
determining certain work hours and standard durations of unit areas
(1 hectare). For this purpose, evaluating the tasks made with human
and machine force from the aspects of duration, productivity and
costs, it has been aimed to determine the most productive method in
accordance with the actual ecological conditions of research field.
Within the scope of the study, the time studies have been conducted
for 3 methods used in weed control efforts. While carrying out those
studies, the performed implementations have been evaluated by
dividing them into business stages. Also, the actual data have been
used while calculating the cost accounts. In those calculations, the
latest formulas and equations which are also used in developed
countries have been utilized. The variance of analysis (ANOVA) was
used in order to determine whether there is any statistically
significant difference among obtained results, and the Duncan test
was used for grouping if there is significant difference. According to
the measurements and findings carried out within the scope of this
study, it has been found during living cover removal efforts in
regeneration efforts in demolished oriental beech forests that the
removal of weed layer in 1 hectare of field has taken 920 hours with
labourer force, 15.1 hours with excavator and 60 hours with an
equipment mounted on a tractor. On the other hand, it has been
determined that the cost of removal of living cover in unit area (1
hectare) was 3220.00 TL for labourer power, 1250 TL for excavator
and 1825 TL for equipment mounted on a tractor.
According to the obtained results, it has been found that the
utilization of excavator in weed control effort in regeneration of
degraded oriental beech regions under actual ecological conditions of
research field has been found to be more productive from both of
aspects of duration and costs. These determinations carried out
should be repeated in weed control efforts in degraded forest fields
with different ecological conditions, it is compulsory for finding the
most efficient weed control method. These findings will light the way
of technical staff of forestry directorate in determination of the most
effective and economic weed control method. Thus, the more actual
data will be used while preparing the weed control budgets, and there
will be significant contributions to national economy. Also the results of this and similar studies are very important for developing the policies for our forestry in short and long term.