Abstract: Cavitation under static negative pressure is not revealed well. The Berthelot method to generate such negative pressure can be a means to study cavitation inception. In this study, metal Berthelot tubes built in observation windows are newly developed and are checked whether high static negative pressure is generated or not. Negative pressure in the tube with a pair of a corundum plate and an aluminum gasket increased with temperature cycles. The trend was similar to that as reported before.
Abstract: Negative pressures of liquids have been expected to contribute many kinds of technology. Nevertheless, experiments for subjecting liquids which have not too small volumes to negative pressures are difficult even now. The reason of the difficulties is because the liquids tend to generate cavities easily. In order to remove cavitation nuclei, an apparatus for enclosing water into a metal Berthelot tube under vacuum conditions was developed. By using the apparatus, negative pressures for water rose to ca. -20 MPa. This is the highest value for water in metal Berthelot tubes. Results were explained by a traditional crevice model. Keywords
Abstract: Thermodynamic properties of liquids under negative pressures are interesting and important in fields of scienceand technology. Here, phase transitions of a thermotropic liquid crystal are investigatedin a range from positive to negative pressures with a metal Berthelot tube using a commercial pressure transducer.Two co-existinglines, namely crystal (Kr) –nematic (N), and isotropic liquid (I) - nematic (N) lines, weredrawn in a pressure - temperature plane. The I-N line was drawn to ca. -5 (MPa).
Abstract: A mathematical model based on a mass and energy
balance for the combustion in a cement rotary kiln was developed.
The model was used to investigate the impact of replacing about
45 % of the primary coal energy by different alternative fuels.
Refuse derived fuel, waste wood, solid hazardous waste and liquid
hazardous waste were used in the modeling. The results showed that
in order to keep the kiln temperature unchanged, and thereby
maintain the required clinker quality, the production capacity had to
be reduced by 1-15 %, depending on the fuel type. The reason for the
reduction is increased exhaust gas flow rates caused by the fuel
characteristics. The model, which has been successfully validated in a
full-scale experiment, was also used to show that the negative impact
on the production capacity can be avoided if a relatively small part of
the combustion air is replaced by pure oxygen.